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Dunn, J., Russell, C., & Morrissey, A. (1999). Remediating historic mine sites in Colorado. Min. Eng., 51(8), 32–35.
Abstract: This article provides examples of reclamation and remediation in Colorado watersheds. The projects were undertaken by the US Environmental Protection Agency (EPA) Region 8, in cooperation with the Colorado Division of Minerals and Geology (CDMG), Colorado Department of Public Health and Environment (CDPHE), US Forest Service (USFS), the Bureau of Land Management (BLM), Bureau of Reclamation (BOR) and the US Geological Survey (USGS). These agencies collaborated on the environmental problems at abandoned mines. These samples involved the interaction of surface and ground waters with sulfide-bearing rocks, mine workings and surface mine spoils that produce acid solutions charged with heavy metals that are toxic to organisms. In these examples, acid mine drainage from historic mines in Colorado has been approached cooperatively with stakeholders. Each example emphasizes one aspect of the three-stage process. These stages include characterization and prioritization, hydrologic controls and the evaluation of long-term remediation activities.
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Ketellapper, V. L., Williams, L. O., Bell, R. S., & Cramer, M. H. (1996). The control of acid mine drainage at the Summitville Mine Superfund Site. In Proceedings of the Symposium on the Application of Geophysics to Environmental and Engineering Problems (SAGEEP), vol.1996 (pp. 303–311).
Abstract: The Summitville Mine Superfund Site is located about 25 miles south of Del Norte, Colorado, in Rio Grande County. Occurring at an average elevation of 11,500 feet in the San Juan Mountain Range, the mine site is located two miles east of the Continental Divide. Mining at Summitville has occurred since 1870. The mine was most recently operated by Summitville Consolidated Mining Company, Inc. (SCMCI) as an open pit gold mine with extraction by means of a cyanide leaching process. In December of 1992, SCMCI declared bankruptcy and vacated the mine site. At that time, the US Environmental Protection Agency (EPA) took over operations of the water treatment facilities to prevent a catastrophic release of cyanide and metal-laden water from the mine site. Due to high operational costs of water treatment (approximately $50,000 per day), EPA established a goal to minimize active water treatment by reducing or eliminating acid mine drainage (AMD). All of the sources of AMD generation on the mine site were evaluated and prioritized. Of the twelve areas identified as sources of AMD, the Cropsy Waste Pile, the Summitville Dam Impoundment, the Beaver Mud Dump, the Reynolds and Chandler adits, and the Mine Pits were consider to be the most significant contributors to the generation of metal-laden acidic (low pH) water. A two part plan was developed to control AMD from the most significant sources. The first part was initiated immediately to control AMD being released from the Site. This part focused on improving the efficiency of the water treatment facilities and controlling the AMD discharges from the mine drainage adits. The discharges from the adits was accomplished by plugging the Reynolds and Chandler adits. The second part of the plan was aimed at reducing the AMD generated in groundwater and surface water runoff from the mine wastes. A lined and capped repository located in the mine pits for acid generating mining waste and water treatment plant sludge was found to be the most feasible alternative. Beginning in 1993, mining wastes which were the most significant sources of AMD were being excavated and placed in the Mine Pits. In November 1995, all of the waste from these sources had been excavated and placed in the the Mine Pits. This paper discusses EPA's overall approach to stabilize on-site sources sufficiently such that aquatic, agricultural, and drinking water uses in the Alamosa watershed are restored and/or maintained with minimal water treatment.
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Stewart, D., Norman, T., Cordery-Cotter, S., Kleiner, R., Sweeney, E., & Nelson, J. D. (1997). Utilization of a ceramic membrane for acid mine drainage treatment. Tailings and Mine Waste '97, , 453–460.
Abstract: BASX Systems LLC has developed a treatment system based on ceramic membranes for the removal of heavy metals from an acid mine drainage stream. This stream also contained volatile organic compounds that were required to be removed prior to discharge to a Colorado mountain stream. The removal of heavy metals was greater than 99% in most cases. A decrease of 30% in chemicals required for treatment and a reduction by more than 75% in labor over a competing technology were achieved. These decreases were obtained for operating temperatures of less than 5 degrees C. This system of ceramic microfiltration is capable of treating many different types of acid mine waste streams for heavy metals removal.
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Davies, G. J., Holmes, M., Wireman, M., King, K., Gertson, J. N., & Stefanic, J. M. (2001). Water tracing at scales of hours to decades as an aid to estimating hydraulic characteristics of the Leadville Mine drainage tunnel.
Abstract: The Leadville Mine Drainage Tunnel (LMDT) is a 3.3 kilometer structure that was constructed in the complicated geology of the Leadville mine district in the 1940's. Discharge from the LMDT is impacted by heavy metals and is treated at a plant built in 1992 operated by the United States Bureau of Reclamation. On the surface waste rock and other remnants of the mining operations litter the landscape and this material is exposed to precipitation. As a result of contact with this material, surface water often has pH of less than 3 and its containment and disposal is necessary before it impacts surface drainage and the nearby Arkansas River. Using a borehole drilled into the mine workings the U.S. EPA has devised a plan in which the impacted water is contained on the surface which then can be discharged into the mine workings to discharge from the LMDT and be treated. The percentage of water discharging from the mining district along the drainage tunnel is unknown, and since there is no access, information about the condition of the tunnel with regards to blockages is also relatively obscure. Application of quantitative water tracing using fluorescent dyes was used to model the flow parameters at the scale of hours in the tunnel and evaluate the likelihood of blockages. Because the tunnel has intersected several lithologies and faults, other locations such as discharging shafts, adits and surface streams that could be hydraulically connected to the LMDT were also monitored. An initial tracer experiment was done using an instantaneous injection, which was followed by additional injections of water. Another tracer injection was done when there was a continuous flow of impacted water into the workings. Analysis of the tracer concentration responses at water-filled shafts and at the portal were used to model the flow along the tunnel and estimate several hydraulic parameters. Waters in these settings are mixtures of components with different residence times, so, qualitative tritium data were used to evaluate residence times of decades. The combined injected tracer and tritium data as well as other geochemical data were used to infer the nature of flow and recharge into the tunnel.
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