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Skousen, J., Rose, A., Geidel, G., Foreman, J., Evans, R., & Hellier, W. (1998). A handbook of technologies for avoidance and remediation of acid mine drainage.
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Mitchell, P., & Wheaton, A. (1999). From environmental burden to natural resource; new reagents for cost-effective treatment of, and metal recovery from, acid rock drainage. In D. E. Goldsack, N. Belzile, P. Yearwood, & G. J. Hall (Eds.), Sudbury '99; Mining and the environment II; Conference proceedings.
Abstract: Acid rock drainage remains the greatest environmental issue faced by the mining sector and as the new millennium approaches, low capital/operating cost treatments remain elusive. Therefore as part of an ongoing process to develop a leading edge, innovative and cost-effective approach, pilot trials were conducted by KEECO in collaboration with the New Bunker Hill Mining Company on a substantial and problematic metal-contaminated acid flow, emanating from underground workings at the Bunker Hill Mine, Idaho. The aims of the work were fourfold. First to assess the capacity of KEECO's unique Silica Micro Encapsulation (SME) reagents and associated dosing systems to cost-effectively decontaminate the acid flow to stringent standards set by the U.S. Environmental Protection Agency (USEPA), where alternative and standard technologies had failed. Second, to demonstrate that treatment using a compact system suitable for underground installation. Third, to demonstrate that the treatment sludge had enhanced chemical stability in absolute terms and relative to standard approaches. Fourth, to examine the potential for resource recovery via sequential precipitation. Although the focus to date has been the development of a cost-effective treatment technology, the latter aim was considered essential in light of the growing pressure on all industrial sectors to develop tools for environmentally sustainable economic growth and the growing demands of stakeholders for improved resource usage and recycling. Two phases of work were undertaken: a laboratory-based scoping exercise followed by installation within the mine workings of a compact reagent delivery/shear mixing unit capable of treating the full flow of 31 L s (super -1) . At a dose rate of 2.0 g L (super -1) (equivalent to a final treated water pH range of 7-9), the SME reagent KB-1 reduced metal concentrations to levels approaching the U.S. Drinking Water Standards, which no other treatment piloted at the site had achieved. Based on the USEPA's Toxicity Characteristic Leaching Procedure, the sludge arising from the treatment was classified as non-hazardous. Operating costs compared favourably with those of lime use, while estimated capital costs were considerably lower due to the compact nature of the reagent delivery system and the rapid settling characteristics of the treatment sediment. Resource recovery was attempted using a two-stage selective precipitation approach. The first stage involved pH adjustment to 5.5 (by addition of 1.5 g L (super -1) of KB-1) to produce a sludge enriched in aluminium, iron and manganese, with lesser amounts of arsenic, nickel, lead and zinc. Further KB-1 addition to a total of 2.1 g L (super -1) generated sludge enriched in zinc (33% by dry weight), demonstrating that resource recovery is theoretically feasible. Further work on downstream processing is required, although it is considered that the most likely route for zinc metal recovery will be high temperature/pressure due to the chemically inert nature of the zinc-rich sediment.
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Mitchell, P., Rybock, J., & Wheaton, A. (1999). Treatment and prevention of ARID using silica micro encapsulation. In S. A. Bengson, & D. M. Bland (Eds.), Proceedings of the 16th annual National meeting of the American Society for Surface Mining and Reclamation; Mining and reclamation for the next millennium (pp. 657–661). 16.
Abstract: In response to the known drawbacks of liming and the ever-increasing regulatory demands on the mining industry, KEECO has developed a silica micro encapsulation (SME) process. SME is a cost-effective, high performance reagent that is utilized in conjunction with simple chemical delivery systems. By encapsulating metals in a silica matrix formation and rapidly precipitating them into a sand-like sludge, it offers all the advantages of liming without the negative drawbacks. Utilizing an injection technique via a high shear mixing device, a slurry from of the SME product called KB-1 (super TM) was applied to ARD at the Bunker Hill Mine in Idaho and to ARD pumped from collection ponds at a remote mine site in the Sierra Nevada Mountains. Flow rates at both sites ranged from 500 to 800 gallons per minute. Treated water from the Bunker Hill Mine operation achieved the site's NPDES criteria for all evaluated metals and U.S. Drinking Water quality for arsenic, cadmium, chromium, lead and zinc with a dosage rate of 1.34 grams KB-1 (super TM) per liter. Treated water from the Sierra Nevada project focused on the control of aluminum, arsenic, copper, iron and nickel. All water samples displayed a >99.5% reduction in these metals, as well as an 84%-87% reduction in the concentration of sulfate. Testing on sludge generated from both operations achieved TCLP Action Limits. The SME process is currently under evaluation as a means to coat the pyrite surfaces of newly generated mine tailings to prevent oxidation and future acid generation.
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Agency, U. S. E. P. (2006). Compost-free bioreactor treatment of acid rock drainage Leviathan Mine, California : innovative technology evaluation report, 2. Cincinnati, OH.: Research Laboratory, Office of Research and Development, United States Environmental Protection Agency.
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Herbert, R. B., Jr., Benner, S. G., & Blowes, D. W. (1998). Reactive barrier treatment of groundwater contaminated by acid mine drainage; sulphur accumulation and sulphide formation. In M. Herbert, & K. Kovar (Eds.), Groundwater Quality: Remediation and Protection (pp. 451–457). IAHS-AISH Publication, vol.250.
Abstract: A permeable reactive barrier was installed in August 1995 at the Nickel Rim Mine near Sudbury, Ontario, Canada, for the passive remediation of groundwater contaminated with acid mine drainage. The reactive component of the barrier consists of a mixture of municipal and leaf compost and wood chips: the organic material promotes bacterially-mediated sulphate reduction. Hydrogen sulphide, a product of sulphate reduction, may then complex with aqueous ferrous iron and precipitate as iron sulphide. This study presents the solid phase sulphur chemistry of the reactive wall after two years of operation, and discusses the formation and accumulation of iron sulphide minerals in the reactive material. The results from the solid-phase chemical analysis of core samples indicate that there is an accumulation of reduced inorganic sulphur in the reactive wall, with levels reaching 190 mu mol g (super -1) (dry weight) by July 1997.
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